Season 2003
Preparations
Target
150+, March 10-14, 2003
Current
activities
The
meeting has been and gone now. The engine conversion, and the
adaption of the gearbox and clutch performed faultlessly, which
was a bonus, as I had not done a conversion like this before. We
had a few difficulties on the way, which I will now mention. On
the Wednesday before the meeting, we took the car to MK
Automotive in Cheltenham to tune the Wolf3D computer I had bought
on Marty's shiny new chassis dyno. If you are thinking of using a
Wolf3D on a 1JZ-GTE, here is a starting map and an engine wiring diagram. It should get the engine
running using the stock sensors. Getting this far on my car took
two weeks. Going through the tuning process, we had done load
points at 4200, about 130 rw kilowatts, and had moved to 4500,
when the engine developed a miss, and started blowing enough oil
smoke to hide the Iraqi army. Remove the plugs and do a
compression test, and the two middle cylinders had lost
compression, one being 25 pounds, the other about 80. Drag the
car home, put it in the shed again, lie on the floor in the
foetal position pounding head on the floor for a couple of hours.
Get up the next morning, ring up the wreckers looking for a cheap
long motor, eventually get one for $550 at Toyospares in
Bayswater. Get it home just after lunch on Thursday, start
pulling the old motor out. Bolt the flywheel, clutch and gearbox
on the new motor, run a compression test, not bad, down on one
cylinder, but too late to care now. Get the motor in on Friday
morning, which was our planned day to leave. Fire the motor, it
runs. Rear turbo oil seals leaking oil into the compressor side,
too late to care now. Start packing all the stuff you need for a
week in the outback with a race (??) car, all packed at about 11
pm. Get up at 6.00 am Saturday, leave. Get to the lake about 3pm
Sunday.
Unpack
the car, set up scrutineering tent, start scrutineering, track
opens about midday Monday 10th of March. The car is running about
130 Mph, which is the same as last year with the 4 cyl. It will
not rev over 5400 rpm. After this, the engine hits a flat spot,
that feels like the key has been turned off. Change to our bigger
tyres and run 136 Mph. We spent a lot of time changing the
computer mapping, thinking that it was because we hadn't mapped
the computer on the dyno over 4500. All this made no difference,
and we were starting to get depressed. It seems that at 5400, the
turbo's are just going into boost. This was very high rpm for no
boost, as on the dyno, at 4500, we were running about 15 PSI of
boost.
Coming
back from another run on the tune up track on Wednesday
afternoon, I was rolling into the pits with the car in neutral,
and the engine idling, when I hear tapping sounds from the
engine. Uh Oh, thats not good. Grab Paul, have a look at things,
and find that the cam pully bolts are loose, and one has been
slipping. Immediate thoughts are for bent springs, piston damage
etc. Turn the cams over, they don't hit anything, Maybe the low
comp turbo motor does not have valve interference. Paul found a
drill the same size of the pin that had fallen out, and we
refitted them. We couldn't find anyone with a comp tester, so we
started the motor, and it ran fine, so out we went. It was now
revving freely, pulling over 7000 in third gear, but not really
pulling in top. We ran 136 Mph, which was our fastest time so
far. On Thursday morning, which was the final session of the
meeting this year, we borrowed a taller set of tyres, and ran 145
Mph. This was our fastest time so far. The boost was just coming
on at about 5500 rpm, although you could hear the whistle well
below this. As well, the intake air temp was very high, above 100
degrees C. We ran three more times that morning, each one a bit
slower than the last. The last run had a very high engine temp,
as the water storage system does not dissipate much heat. When we
got back to civilisation, and had mobile phone coverage again, I
had a message to say that Marty had found bits if turbo in his
workshop, which means that they are no longer where they should
be. From this, I assume that one turbo was not doing much. It
also seems that my cold air intakes and intercooler ducts were
not very effective. I suspected that they may be in a low
pressure area on the body, but had no way of telling if this was
the case or not. What I think is required is a scoop at least 6
inches above the body in the clean air, sort of like what the
open wheel race cars run. One of the other things that will be
looked at is some way of dropping hot water from the coolant
storage tank, and letting somecold water in, to let us run more
often. At the moment, I think I will use self sealing air
fittings.
At least
we are going up in speed. I will pull the two motors down over
the next 4 weeks or so, and have a look at what is bringing the
compression down. I hope it will not be something too serious,
and look towards next year with a fresher motor, and a single
turbo.
As we
say in Empty Pockets racing, There's always next year (2004)
The car is at home and has been dismanteled. I have
cut the frame and added another 2 feet in length. The engine has
been adapted to the gearbox, less clutch. The rear radius rods
have been re attached to the frame in their new position. As the
engine sits higher than before, the diff has been lifted by half
an inch to suit. I reversed the old transmission mount and found
that it suits the new engine position. Some new engine mount
brackets have been added to the frame.
Things done.
Cut the tank and add 2 feet
behind the drivers capsule. Done
Mount the engine and adapt it to
the gearbox. (Done)
New fuel tank with a high
pressure efi pump. I hav one from a Volvo as a main pump, and a
Toyota that I could use as a pre pump if required. The fuel
system is very compact, so I am hoping that the lack of
restriction in the lines will help as well.
Make new manifold to move the
turbos up.
Make a remote oil filter
adapter. The oil filter wants the same spot as the frame rail.
(No longer required. By rotating the oil filter adapter the
filter fits between the rails.
I do have to make a retainer for it now)
Find some way to get airflow through the intercooler.
Built a water storage system to
replace the radiator, which was inadequate with the 4 cyl.
Upgrade the steering, I think it
could be a bit marginal at high speed.
I will also need to put in some instrumentation.
Exhaust gas temp, Oil pres, Water temp, Intercooler temp, fuel
pressure. I have no idea where they will go. My intention now is
to use the hand controller form the Wolf3D to supply most of
these. I am not yet quite sure how the computer works out when
No. 1 is at top dead centre.
The ignition will run in 3 pairs with a wasted spark. The
injectors will also run in 3 pairs.
 |
Well here is the new engine. 1JZ-GTE Specs: 2491cc
EFI DOHC 24-valve 6cyl twin turbo
Power: 208kW @6200rpm
Torque: 362Nm @4800rpm
Gearboxes: RWD 5-speed and 4 speed auto
Vehicles: Supra 2.5GT 91-93. Toyota Soarer
The engine needs to mount a lot lower than this, so
the turbos have to be moved
|
| For the 1JZ, some more power can be
obtained by removing the exhaust restictions (no problem
here) which will up the boost a bit. More than this and a
bigger single turbo and intercooler is required. The
injectors, intercooler and turbo seem to be well matched,
and max out at about the same output. The factory
intercooler is a perfect size for the lakester, being
about 10 inches square, and about 4 inches thick. It is
constructed like a radiator, with cast aluminium ends.
Two of these in parallel would probably be ideal from a
size point of view, and OK for the amount of power to be
extracted from this model. |
 |
The frame was mounted to a table normally used for A
Model frames. The front half is welded in place, and the
rear half is mounted by brackets that I can move and
clamp in a new position. I put in some bracing to keep
everything lined up when the cuts were made. |
 |
The frame was cut at an angle to give more weld on
the join. I had a lot of trouble finding something
suitable to use as a sleeve for the joins. In the end I
had to buy some thickwall seamless tube, and then turn it
down to the right size. As the bottom frame rails are not
quite parallel to the top rails, there was a bit of
stuffing around to get the tubes lined up with each
other. |
 |
Once the tubes were connected, I used an endless
chain and a large hammer to draw the two sections
together. Some heavy tack welds were applied, and the
frame was then returned home. Nothing further has
happened, as it was at this pont that I injured my
fingers, and nothing can happen now until I get the use
of them back. |
 |
The engine I have is out of a Soarer. 95% of these
were auto. Therefore, I need to adapt the manual that the
car is setup for, to the engine. Looking at the two
bellhousings side by side, the Soarer auto one is about
an inch shorter. I think an adapter plate can be made to
mate the gearbox to the auto bellhousing. The clutch will
be a problem to solve. |
 |
The adapter needs to be almost an inch thick. I was
going to get it made from a piece of thick plate, but
then I thought that I mught have a go myself. I modified
my lathe (a 1930's flat belt Colchester) with some
stepdown pulleys, and using the back gear, I can get it
down to about 45 RPM. This is what I need to get the
cutting speed down to something that won't melt the
tools. I cut a bit of 6 mm plate that was left over from
when the car was built, and bolted it to the backing
plate that normally holds the chuck. I then turned a hole
that would hold the input shaft retainer from the gear
box. The blue dots are where the bellhousing bolts, and
need to be threaded. The red crosses are where the
adapter mounts to the gearbox. It all looks like it will
work so far |
 |
The next step was to bend some 10 mm square in an
approximatly circular shape of about 9 inch diameter.
This ring will be between the rear 6mm plate, and the
front 10 mm one. I then cut a ring with two ears on it
from a piece of 10 mm plate, and welded the ring to it.
This was then placed on the piece of 6mm plate, and
welded to it. |
 |
The assembly was mounted in the lathe again, and the
face was turned true, with a lip to hold the bellhousing.
This took a while, as the lathe can't take much of a cut,
and has some teeth missing on the cross slide feeder, and
needs to be prompted by hand after about half an inch. |
 |
Once I was happy with that, I removed it from the
lathe, trimmed the excess, and smoothed the sharp edges
with a sander. I then clamped the bellhousing to it, and
used it as a jig to locate the holes. The six holes have
been drilled and tapped. I then faced the other side in
the lathe, and bolted the gearbox to the motor. There is
no provision for a clutch yet. One step at a time. |
 |
The manifolds for the turbos are being made out of 42
mm steam bends and tube. I used a hole saw in the lathe
to fit the tubes together. There is a bit too much
movement in the bed of the lathe to do it properly, so
now 2 hole saws have joined their maker. |
 |
The coolant storage tank is about 90 per cent
complete, with inlets/outlets and the area under the
intercooler to be finished. This will wait until the
intercooler is complete, to make sure that it mounts ok,
and doesn't foul anything. |
 |
The intercooler fits nicely. Fellow DLRA member
Graeme Holden has welded two stock Soarer units together.
He works at AVO Turboworld just down the road here, and
has done a magnificant job. |
 |
I also have to make a new clutch fork, as my gearbox
adapter fouls the existing one. |
 |
This is the start of the new dump pipes. Seperate
pipes for each turbo and waste gate. |
 |
I have made a roller and rolled the extension needed
for the bottom of the tank. No work on the upper body
work yet |
 |
I have made a clutch fork out of a piece of 100 by 20
mm bar. I looked at bending the old one to suit, but I
thought the risk of it breaking under load was too high. |
 |
A lot of machining, grinding, filing, drilling,
sanding, heating and bending went on here to get this. |
 |
The finished item. Seems to act OK, but I wont really
know until I get the finished items installed. |
 |
I redid the turbo end of the manifolds to pull them
within the body. Once I had rotated the compressor
housings, there was plenty of room to tuck everything in. |
 |
I have made up some sheet metal to extend the body.
There needs to be a bulge towards the rear of this to fit
the intercooler, and some way of pulling air into the
intercoolers. I have made a seperate pipe for each turbo
outlet, and each wastegate output as well. |
 |
When the rack was turned to full right, the end of
the rack was loose in the housing because the gear part
of the rack was now in the end housings. I welded some
metal that I had roughly shaped with a grinder to the end
of the gear part. |
 |
Once welded, and turned on the lathe, the problem was
fixed. It removed about 40mm of travel, but I wasn't
using that part of the rack anyway. The rack did slightly
pull in the welding, but because the housing is so short,
it has made no difference to the operation. |
 |
I shortened the rack severely. I tried a Mazda 323
rack, but when it was shortened, it was very hard to hold
in position, and the pinion angle was poorly placed. The
Morris Minor rack (the top one) was much more suitable,
but I didn't want to shorten it because it is the spare
for my roadster. Too late now as it has been cut down so
severly to fit in, the two end housings virtually touch. |
 |
The finished (almost) steering. I need to obtain a
bearing to support the bottom of the column. I hope for a
large improvement in steering feel, and a lot faster
reaction to wind gusts now. Last year, the car had moved
about 20 or 30 feet before the play in the box was taken
up. |
 |
I have my new flywheel and clutch. 19 kilograms.
Throttle response is not going to be much to brag about,
but I am hoping that it may smooth out the top end (not
that a Toyota would need that), and add that extra MPH.
The clutch is a 5 puck solid center item. Doesn't seem
too grabby. |
 |
I have made some bulges to cover the intercoolers.
Next on the list is some way of getting the air into the
intercoolers. |
 |
I wanted to install a fuel pressure guage, but I
couldn't get a banjo bolt with a double hole in it with
the right thread. I bought a standard high tensile bolt,
drilled two holes across it, then chucked it in the lathe
and centre drilled it. I then silver soldered a bit of
pipe to a standard banjo fitting, and used an oil
pressure sensor from a VK Commodore. I also used one of
these as the oil pressure sender, as the Toyota only has
a light. These VDO items are ridiculously cheap at the
wreckers, much cheaper than new items. I used a toggle
switch to switch between oil and fuel pressure. |
 |
This is the turbo pipe work. Mandrel bends, and step
ups were used here. Tacked together with a MIG, and
fusion welded with an oxy. |
 |
I have added the air intakes for the intake and the
intercooler. As it turned out, they are not really in the
air flow |
| |
|
| |
|
| |
|
Updated
17/Mar/03
You can E-mail me at: